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Nitretação Sob Plasma Por Tela Ativa E Plasma Direto/dc Do Aço Inoxidável Endurecível Por Precipitação Tipo 17-4 PhBy Amanda de Angelis Vitoi
A nitretação do aço inoxidável endurecível por precipitação do tipo 17-4PH foi estudada comparativamente pelos processos de Plasma-DC e de Tela Ativa. Os resultados mostram que os dois processos são e
Aug 16, 2017
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Nitric Acid in the Hydrometallurgy of SulfidesBy Fathi Habashi
Nitric Acid has been used for over 50 years in the uranium industry and in phosphate fertilizer manufacture. Its application in the treatment of sulfide concentrates is relatively recent. A review of
Jan 1, 1999
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Nitric Acid Leaching for Pre-Treatment of a Copper Bearing Auroferrous Pyritic ConcentrateBy P. Altinkaya, O. Celep, H. Deveci, E. Y. Yazici
"Copper-bearing gold ores have proved difficult to treat in conventional cyanide leaching process owing to prohibitively high consumption of cyanide by readily soluble copper minerals interfering with
Jan 1, 2018
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Nitric Acid Pretreatment Applied to a Refractory Gold‑Tellurides Ore - Mining, Metallurgy & Exploration (2023)By Dairo E. Chaverra, Carlos Argumedo‑Jimenez, Oscar J. Restrepo‑Baena
This paper presents the results obtained by processing a gold and silver telluride mineral concentrate from a mine in Colombia. An acid wash, also known as acidification, was carried out, followed by
Nov 8, 2023
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Nitric-Sulfuric Leach Process ImprovementsBy D. S. Davies
Further development of the Nitric-Sulfuric Leach (NSL) process has led to an improved design of the leach and nitric acid recovery steps. NO produced in the leach step is reacted with oxygen, regenera
Jan 1, 1978
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Nitriding Of Ilmenite And High-Grade Slag Fines ? SynopsisBy D. S. van Vuuren
Titanium bearing resources can selectively be chlorinated at temperatures below 200°C if the Ti02 in the feed is nitrided before chlorination. However, the nitriding reaction is highly endothermic, re
Jan 1, 2011
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Nitrogen Control in the EAF and Post EAF ProcessesBy B. Stettner, J. Asante, S. Abraham
The levels of nitrogen in steel produced in various metallurgical vessels vary significantly. For example, the tap nitrogen levels in steel produced in the BOF are around 4Oppm, as compared to 70-100p
Jan 1, 2004
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Nitrogen Inertization At San Juan Coal Company’s Longwall OperationBy Jacques F. Abrahamse, Kevin A. Bahe, T. Arthur Palm, Gregory E. McCluskey, Stephen L. Bessinger
Introduction Basis For System San Juan Coal Company (SJCC) is a subsidiary of BHP Billiton. Until recently, BHP Billiton operated three surface mines in northwestern New Mexico: Navajo, San Juan,
Jan 1, 2005
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Nitrogen Solubility In Molten CaO-SiO2 SlagsBy H. G. Oltmann
The equilibrium nitrogen solubility in the CaO-SiO2system was studied by a slag-gas equilibration technique, in graphite crucibles at 1823K under a CO-N2 atmosphere. The nitrogen content of the slags
Jan 1, 1999
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Nitrogen-Based Collectors for Sulfide Flotation – Tecflote™By A. Lewis, J. Zachwieja, M. Widell, P. Zhou, W. W. Geissler, M. Svensson, A. Movahedi, H. Nordberg
Flotation collectors for sulfide minerals has been traditionally based on xanthate, thiophosphate, thiophosphinate and thiocarbamate, all derived from sulfur chemistry. Tecflote™ is a new family of pa
Jan 1, 2019
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NMA’s MINExpo ’96 Plans for 30,000 People and More Than 900 ExhibitorsThe National Mining Association’s (NMA)MINExpo International ’96 is shaping up to be the organization’s largest. About 30,000 mining industry business and technical professionals are expected to desc
Jan 1, 1996
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No entry mechanised presink of the Wira Hoisting ShafBy D Kilkenny
This paper discusses the use of a mechanised shaft sinking machine Herrenknecht Vertical Shaft Sinking Machine (VSM) – to conduct the 93 m presink for the Wira Hoisting Shaft at the Prominent Hill Min
Mar 29, 2023
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No Net Loss and Offsite Mitigation: Is New Zealand Mature Enough for a Win-Win Situation?By S Christensen
In August 2001 the Minister for Conservation declined an application by GRD Macraes for an access arrangement to enable work at the Globe Progress Mine near Reefton. In her decision, Ms Lee said:æI ha
Jan 1, 2002
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No. 2 Open Hearth Plant at Port KemblaBy Edmonds W, Jeffcoat R
The completion of the first two open hearth furnaces in the new No. 2 open hearth plant at Port Kembla will increase Australian production of steel by 350,000 tons of ingots per annum.The paper gives
Jan 1, 1957
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No. 3 ChangehouseWith the sinking of the No. 3 Shaft at North Broken Hill Limited, it was necessary to construct adjacent to the shaft a new changehouse for mining and surface personnel.It was also probable that as th
Jan 1, 1957
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No. 3 HeadframeTo finalise the arrangement and details of the headframe to be erected over the new No. 3 Shaft, the haulage and winding equipment requirements were first determined, then tentative designs were prepa
Jan 1, 1957
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No. 3 Shaft Sub-Brace AreaWith the sinking of the No. 3 Shaft and the erection of a changehouse nearby, a sub-brace level structure was provided incorporating a time office, underground foremenÆs office and lamp room, in conju
Jan 1, 1957
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No. 3 Shaft Winders and Winder HouseThe sinking of the new No. 3 Shaft being mainly concerned with providing for the continuation of mining operations north of the existing workings, requirements for the shaft and haulage equipment were
Jan 1, 1957
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No. 3 Tankhouse at Onahama Smelter and RefineryBy H. Ikeda
The new Onahama N0.3 tankhouse was put into operation early in 1973. This new tankhouse, which has a capacity of 90,000 metric ton cathode per year, is distinct in many important respects from convent
Jan 1, 1976
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No. 3 Ventilation Shaft: Shaft-Sinking EquipmentWith the sinking of the new No. 3 Shaft and the increasing depth and northward movement of the mining operations, improved ventilation of the mine workings became necessary and it was decided to sink
Jan 1, 1957